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64 WORKING SMARTER: REDUCING NOx EMISSIONS IN MULTIPLE HEARTH INCINERATORS BY IMPROVED OPERATING TECHNIQUES James P. Scisson, Jr., Operations Specialist Felix F. Sampayo, Senior Vice President Gary A. Goldberg, Director, Construction Services Jones & Henry Engineers, Inc. Toledo, Ohio 43606 Michael Heitz, Assistant Superintendent Metropolitan Sewer District of Greater Cincinnati Cincinnati, Ohio 45204 INTRODUCTION Working harder, although a virtue, may not be the best way to solve a problem. Solutions to many difficult problems are found by working smarter. A team of engineers, programmers, and operators dramatically improved the performance of incinerators at the Metropolitan Sewer District (MSD) of Greater Cincinnati Mill Creek Wastewater Treatment Plant. Modifications to the original operating scheme resulted in the incinerators meeting NOx emission limits that were not contemplated at the time of design. As a side benefit, particulate emissions and fuel consumption were reduced significantly from previous values. BACKGROUND In August 1982, the MSD retained Jones & Henry Engineers, Inc. to prepare a Diagnostic Evaluations and Composite Correction Program for the 120-MGD Mill Creek Wastewater Treatment Plant. As part of the improvements, MSD constructed two additional multiple hearth incinerators (MHIs) and rehabilitated the four existing ones. Design began in June 1984; construction in 1986. Each incinerator is a 22 ft, 3-in., 9-hearth unit with a capacity of 9.4 wet tons/hr (Figure 1). The units are "typical" MHIs and have burners on the odd-numbered (out) hearths. The air pollution control equipment for the two new units (Incinerators 5 and 6) consists of venturi scrubbers followed by a three-tray impingement scrubber. Afterburners were provided for the new units to meet expected future regulations. The four original units (Incinerators 1-4) have a three-tray impingement scrubber with an air bleed inlet damper to maintain constant gas flow and differential through the scrubber. All induced draft fans have variable frequency drives for draft control. The incinerators are controlled by a Programmable Logic Controller (PLC) system which provides automatic operation with little need for operator intervention At the time of design and construction there was no limit on NOx emissions. The requirements changed before startup. The Mill Creek Incinerators are required to comply with emission limits of 1.1 lb/particulate per dry ton of sludge burned and 5.0 lb NOx per dry ton of sludge burned. The NO„ limit was triggered by the need to maintain National Ambient Air Quality Standards for NOx, and to prevent significant deterioration of the air quality. USEPA publication AP-42 NOx emission factors were used by the regulatory agency to estimate NOx emissions. To the best of our knowledge this is the first enforced NOx permit limit applied to MHIs in the United States. The two new incinerators were placed in service after a protracted construction period. The construction delays were due to the subsequent bankruptcies of two general contractors on the project. Emission testing in August 1990 produced NOx levels 300% of permit.' The incinerators were ordered to shut down after failing their emissions test. 47th Purdue Industrial Waste Conference Proceedings, 1992 Lewis Publishers, Inc., Chelsea, Michigan 48118. Printed in U.S.A. 591
Object Description
Purdue Identification Number | ETRIWC199264 |
Title | Working smarter : reducing NOx emissions in multiple hearth incinerators by improved operating techniques |
Author |
Scisson, James P. Sampayo, Felix F. Goldberg, Gary A. Heitz, Michael |
Date of Original | 1992 |
Conference Title | Proceedings of the 47th Industrial Waste Conference |
Conference Front Matter (copy and paste) | http://e-archives.lib.purdue.edu/u?/engext,43678 |
Extent of Original | p. 591-598 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital object copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Date Digitized | 2009-12-10 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Resolution | 300 ppi |
Color Depth | 8 bit |
Description
Title | page 591 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Transcript | 64 WORKING SMARTER: REDUCING NOx EMISSIONS IN MULTIPLE HEARTH INCINERATORS BY IMPROVED OPERATING TECHNIQUES James P. Scisson, Jr., Operations Specialist Felix F. Sampayo, Senior Vice President Gary A. Goldberg, Director, Construction Services Jones & Henry Engineers, Inc. Toledo, Ohio 43606 Michael Heitz, Assistant Superintendent Metropolitan Sewer District of Greater Cincinnati Cincinnati, Ohio 45204 INTRODUCTION Working harder, although a virtue, may not be the best way to solve a problem. Solutions to many difficult problems are found by working smarter. A team of engineers, programmers, and operators dramatically improved the performance of incinerators at the Metropolitan Sewer District (MSD) of Greater Cincinnati Mill Creek Wastewater Treatment Plant. Modifications to the original operating scheme resulted in the incinerators meeting NOx emission limits that were not contemplated at the time of design. As a side benefit, particulate emissions and fuel consumption were reduced significantly from previous values. BACKGROUND In August 1982, the MSD retained Jones & Henry Engineers, Inc. to prepare a Diagnostic Evaluations and Composite Correction Program for the 120-MGD Mill Creek Wastewater Treatment Plant. As part of the improvements, MSD constructed two additional multiple hearth incinerators (MHIs) and rehabilitated the four existing ones. Design began in June 1984; construction in 1986. Each incinerator is a 22 ft, 3-in., 9-hearth unit with a capacity of 9.4 wet tons/hr (Figure 1). The units are "typical" MHIs and have burners on the odd-numbered (out) hearths. The air pollution control equipment for the two new units (Incinerators 5 and 6) consists of venturi scrubbers followed by a three-tray impingement scrubber. Afterburners were provided for the new units to meet expected future regulations. The four original units (Incinerators 1-4) have a three-tray impingement scrubber with an air bleed inlet damper to maintain constant gas flow and differential through the scrubber. All induced draft fans have variable frequency drives for draft control. The incinerators are controlled by a Programmable Logic Controller (PLC) system which provides automatic operation with little need for operator intervention At the time of design and construction there was no limit on NOx emissions. The requirements changed before startup. The Mill Creek Incinerators are required to comply with emission limits of 1.1 lb/particulate per dry ton of sludge burned and 5.0 lb NOx per dry ton of sludge burned. The NO„ limit was triggered by the need to maintain National Ambient Air Quality Standards for NOx, and to prevent significant deterioration of the air quality. USEPA publication AP-42 NOx emission factors were used by the regulatory agency to estimate NOx emissions. To the best of our knowledge this is the first enforced NOx permit limit applied to MHIs in the United States. The two new incinerators were placed in service after a protracted construction period. The construction delays were due to the subsequent bankruptcies of two general contractors on the project. Emission testing in August 1990 produced NOx levels 300% of permit.' The incinerators were ordered to shut down after failing their emissions test. 47th Purdue Industrial Waste Conference Proceedings, 1992 Lewis Publishers, Inc., Chelsea, Michigan 48118. Printed in U.S.A. 591 |
Resolution | 300 ppi |
Color Depth | 8 bit |
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