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68 CONTROL OF CARBIDE LEVELS IN DESULFURIZATION OF GREY IRON SO SLAG WILL BE NON-HAZARDOUS James E. Etzel, Professor School of Civil Engineering Purdue University West Lafayette, Indiana 47907 William Kodatsky, Product Manager Cyanamid Canada, Inc. Markham, Ontario Canada L3P 3J5 Joseph B. Medved, Administrator Environmental Activities General Motors Corporation Saginaw, Michigan 48605 INTRODUCTION In order to produce the quality of product required for nodular iron castings, the normal sulfur level of grey iron must be reduced. To achieve the reduction, it is desirable to use calcium carbide to destroy or liberate the sulfur from the molten iron. The initial efforts which were to be accomplished were to treat the carbide containing slag with an excess of a sulfur compound. This treatment was intended to drive the reaction with the carbide to completion. The treatment should have left no residual carbide to produce acetylene on contact with moisture from the air or from water quenching of the slag. By driving the reaction to the point of zero residual carbide, where acetylene generation would not be possible, the slag would not be a hazardous waste. The actual form of the sulfur in the metal was unsure. This made it unclear whether the carbide destruction of sulfur was an oxidative or a reductive process. In view of this fact, two forms of excess sulfur to drive the reaction to the point of zero carbide residual were considered for use. One was calcium sulfate and the other sodium hydro- sulfide. Prior to testing of the proposed procedures for sulfur addition, the program was modified by the introduction of a new modified calcium carbide. The material, produced by Cyanamid Canada, Inc., was a new compounded form of carbide with properties which allowed it to approach total consumption during the desulfurization process, thus minimizing any excesses in the resulting slag. In view of the promise of this material, the testing was redirected to evaluations of modified calcium carbide residuals obtainable in actual full scale desulfurization trials. A test procedure for acetylene generation potential of a slag had been developed by Cyanamid Canada. When subjected to a close evaluation, this procedure proved to be less sensitive than required. A new testing procedure, using a portable gas chromatograph and a trapped volume of air, was evolved. This procedure was to be sensitive enough to measure the levels of acetylene at 1.0% or less of the lower explosive limit (LEL). The details of the procedure will be presented later in this chapter. The final part of the effort was to run acetylene measurements on slag samples from test runs of the desulfurization procedure using the modified carbide. Data from these tests were developed and compared with the desired levels of acetylene as established by a consensus of General Motors Corporation staff and other parties associated with the evaluation program. An agreed acetylene level was necessitated by the absence of any specifics on acetylene in the RCRA regulations. Other than the flammable-explosive classification which applied, no specifics on acetylene were found to be available. In order to arrive at an agreed acetylene level, many factors regarding the desulfurization process and its operation had to be considered. 43rd Purdue Industrial Waste Conference Proceedings, © 1989 Lewis Publishers, Inc., Chelsea, Michigan 48118. Printed in U.S.A.
Object Description
Purdue Identification Number | ETRIWC198868 |
Title | Control of carbide levels in desulfurization of grey iron so slag will be non-hazardous |
Author |
Etzel, James E. Kodatsky, William Medved, Joseph B. |
Date of Original | 1988 |
Conference Title | Proceedings of the 43rd Industrial Waste Conference |
Conference Front Matter (copy and paste) | http://e-archives.lib.purdue.edu/u?/engext,39828 |
Extent of Original | p. 593-604 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital object copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Date Digitized | 2009-08-14 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Resolution | 300 ppi |
Color Depth | 8 bit |
Description
Title | page 593 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Transcript | 68 CONTROL OF CARBIDE LEVELS IN DESULFURIZATION OF GREY IRON SO SLAG WILL BE NON-HAZARDOUS James E. Etzel, Professor School of Civil Engineering Purdue University West Lafayette, Indiana 47907 William Kodatsky, Product Manager Cyanamid Canada, Inc. Markham, Ontario Canada L3P 3J5 Joseph B. Medved, Administrator Environmental Activities General Motors Corporation Saginaw, Michigan 48605 INTRODUCTION In order to produce the quality of product required for nodular iron castings, the normal sulfur level of grey iron must be reduced. To achieve the reduction, it is desirable to use calcium carbide to destroy or liberate the sulfur from the molten iron. The initial efforts which were to be accomplished were to treat the carbide containing slag with an excess of a sulfur compound. This treatment was intended to drive the reaction with the carbide to completion. The treatment should have left no residual carbide to produce acetylene on contact with moisture from the air or from water quenching of the slag. By driving the reaction to the point of zero residual carbide, where acetylene generation would not be possible, the slag would not be a hazardous waste. The actual form of the sulfur in the metal was unsure. This made it unclear whether the carbide destruction of sulfur was an oxidative or a reductive process. In view of this fact, two forms of excess sulfur to drive the reaction to the point of zero carbide residual were considered for use. One was calcium sulfate and the other sodium hydro- sulfide. Prior to testing of the proposed procedures for sulfur addition, the program was modified by the introduction of a new modified calcium carbide. The material, produced by Cyanamid Canada, Inc., was a new compounded form of carbide with properties which allowed it to approach total consumption during the desulfurization process, thus minimizing any excesses in the resulting slag. In view of the promise of this material, the testing was redirected to evaluations of modified calcium carbide residuals obtainable in actual full scale desulfurization trials. A test procedure for acetylene generation potential of a slag had been developed by Cyanamid Canada. When subjected to a close evaluation, this procedure proved to be less sensitive than required. A new testing procedure, using a portable gas chromatograph and a trapped volume of air, was evolved. This procedure was to be sensitive enough to measure the levels of acetylene at 1.0% or less of the lower explosive limit (LEL). The details of the procedure will be presented later in this chapter. The final part of the effort was to run acetylene measurements on slag samples from test runs of the desulfurization procedure using the modified carbide. Data from these tests were developed and compared with the desired levels of acetylene as established by a consensus of General Motors Corporation staff and other parties associated with the evaluation program. An agreed acetylene level was necessitated by the absence of any specifics on acetylene in the RCRA regulations. Other than the flammable-explosive classification which applied, no specifics on acetylene were found to be available. In order to arrive at an agreed acetylene level, many factors regarding the desulfurization process and its operation had to be considered. 43rd Purdue Industrial Waste Conference Proceedings, © 1989 Lewis Publishers, Inc., Chelsea, Michigan 48118. Printed in U.S.A. |
Resolution | 300 ppi |
Color Depth | 8 bit |
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