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62 ENHANCED TREATMENT OF HIGH STRENGTH SOFT DRINK BOTTLING WASTEWATERS James C. O'Shaughnessy, Professor and Head Department of Civil Engineering Worchester Polytechnic Institute Worchester, Massachusetts 01609 Frederic C. Blanc, Professor Department of Civil Engineering Northeastern University Boston, Massachusetts 02115 Steven H. Corr, Vice President Alejandro Toro, Engineer Weston and Sampson Engineers, Inc. Wakefield, Massachusetts 01880 INTRODUCTION The Coca Cola Bottling Company of Cape Cod began production at a new facility in Sandwich, Massachusetts in 1984. The Department of Environmental Quality Engineering required that the company construct an on-site treatment facility to handle the discharge from the bottling operation. That facility was designed to achieve effluent quality of less than 20 mg/L BOD5 and TSS prior to discharging into the ground.1 The industrial wastewater treatment facility was constructed in early 1984 and placed on line in June of that year. The plant consisted of the following: 1. Two lined lagoons with a volume of 267,800 gallons each providing a detention time of 30 days at summer design flow. The lagoons were designed to operate in series and were aerated through a diffused fine bubble aeration system. 2. Two rapid infiltration basins for effluent disposal. The basins were designed based on a percolation rate of 4 gallons per day per square foot. Chemical feed equipment was provided for the addition of nutrients. Nitrogen and phosphorus were added after the initial start up of the plant. pH neutralization for the system using 50% caustic soda was also provided. The design of the wastewater treatment system was based on pilot plant work conducted on the wastewater effluent from the old production facility in South Sagamore.1 That work indicated that a thirty-day detention time with aeration would reduce the influent BOD from 1200 mg/L to between 5 and 10 mg/L. Based on that pilot plant study, the design parameters shown in Table I were established. BACKGROUND Following start up of the plant in the summer of 1984, several operational problems were experienced which prevented the facility from meeting the groundwater discharge permit limits of 20 mg/L for BOD and TSS. The first problem encountered involved the complete destruction of all bacteria in the facility due to failure of a valve on a caustic line. The pH of the wastewater increased to over 12 following the inadvertent dumping of 700 gallons of 50% caustic into the lagoons. The treatment plant was neutralized with sulfuric acid and restarted using an inoculation of bacteria. 607
Object Description
Purdue Identification Number | ETRIWC198762 |
Title | Enhanced treatment of high strength soft drink bottling wastewaters |
Author |
O'Shaughnessy, James C. Blanc, Frederic C. Corr, Steven H. Toro, Alejandro |
Date of Original | 1987 |
Conference Title | Proceedings of the 42nd Industrial Waste Conference |
Conference Front Matter (copy and paste) | http://e-archives.lib.purdue.edu/u?/engext,38818 |
Extent of Original | p. 607-618 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital object copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Date Digitized | 2009-08-03 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Resolution | 300 ppi |
Color Depth | 8 bit |
Description
Title | page 607 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Transcript | 62 ENHANCED TREATMENT OF HIGH STRENGTH SOFT DRINK BOTTLING WASTEWATERS James C. O'Shaughnessy, Professor and Head Department of Civil Engineering Worchester Polytechnic Institute Worchester, Massachusetts 01609 Frederic C. Blanc, Professor Department of Civil Engineering Northeastern University Boston, Massachusetts 02115 Steven H. Corr, Vice President Alejandro Toro, Engineer Weston and Sampson Engineers, Inc. Wakefield, Massachusetts 01880 INTRODUCTION The Coca Cola Bottling Company of Cape Cod began production at a new facility in Sandwich, Massachusetts in 1984. The Department of Environmental Quality Engineering required that the company construct an on-site treatment facility to handle the discharge from the bottling operation. That facility was designed to achieve effluent quality of less than 20 mg/L BOD5 and TSS prior to discharging into the ground.1 The industrial wastewater treatment facility was constructed in early 1984 and placed on line in June of that year. The plant consisted of the following: 1. Two lined lagoons with a volume of 267,800 gallons each providing a detention time of 30 days at summer design flow. The lagoons were designed to operate in series and were aerated through a diffused fine bubble aeration system. 2. Two rapid infiltration basins for effluent disposal. The basins were designed based on a percolation rate of 4 gallons per day per square foot. Chemical feed equipment was provided for the addition of nutrients. Nitrogen and phosphorus were added after the initial start up of the plant. pH neutralization for the system using 50% caustic soda was also provided. The design of the wastewater treatment system was based on pilot plant work conducted on the wastewater effluent from the old production facility in South Sagamore.1 That work indicated that a thirty-day detention time with aeration would reduce the influent BOD from 1200 mg/L to between 5 and 10 mg/L. Based on that pilot plant study, the design parameters shown in Table I were established. BACKGROUND Following start up of the plant in the summer of 1984, several operational problems were experienced which prevented the facility from meeting the groundwater discharge permit limits of 20 mg/L for BOD and TSS. The first problem encountered involved the complete destruction of all bacteria in the facility due to failure of a valve on a caustic line. The pH of the wastewater increased to over 12 following the inadvertent dumping of 700 gallons of 50% caustic into the lagoons. The treatment plant was neutralized with sulfuric acid and restarted using an inoculation of bacteria. 607 |
Resolution | 300 ppi |
Color Depth | 8 bit |
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