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EXTENDED AERATION OF COKE-PLANT EFFLUENTS J. Ganczarczyk, Professor D. Elion, Project Engineer Department of Civil Engineering University of Toronto Toronto, Canada M5S 1A4 INTRODUCTION Activated sludge treatment of coke-plant effluents differs substantially from such treatment of sewage and many industrial wastewaters because of concentration and characteristic composition of these effluents. Biological treatment plants for coke-plant effluents are not very numerous but the technologies applied by these plants and their operation patterns also differ markedly. The activated sludge treatment plant at Dominion Foundries and Steel Limited (DOFASCO) in Hamilton, Ontario is the only Canadian plant and one of the few North American plants for treatment of coke-plant effluents. This plant is unique in its own kind because it operated without any intentional removal of excess activated sludge. During its history, the DOFASCO plant underwent few changes and in the year 1975 its aeration tank volume was doubled. The characteristic performance of this plant prior to this change and afterwards is the subject of this study. WASTEWATER ORIGIN AND GENERAL CHARACTERISTICS The coke plant at the Dominion Foundries and Steel Limited (DOFASCO) in Hamilton, Ontario produced in 1975 an average of 3,680 t/day (3,340 kkg/day) of metallurgical coke from a low-sulfur West Virginia coal. The following streams of wastewater containing phenolics and thiocyanate were collected: excess crude flushing liquor, condensate from the collection mains, condensate from primary coolers and condensate from the light oil plant. The flow of these effluents ranged from 4,700 to 10,000 US gal per hr (17.8-37.9 m3/hr) and was a function of coal moisture contents and connection of new wastewater streams to the system. These effluents were originally equalized in a storage tank of 425,000 US gal (1,609 m3) volume, which also provided a separation of residual tar. The next step of pretreatment (Figure 1) was ammonia stripping in a free-and-fixed- leg Koppers still, installed in 1971. The ammonia stripping was performed with lime addition to raise pH over 9.5, and by addition of low pressure steam at a rate of 9,000-12,000 lb/hr (4,086-5,448 kg/hr), and high-pressure steam at the rate of 700- 1,000 lb/hr (318-454 kg/hr). The additions of slaking water and steam condensates provided a 30 to 40% dilution of the wastewater. The wastewater discharged from the still had temperature in the range of 210 F (99 C), and thus required cooling during the summer through heat exchangers using bay water. A 200,000 US gal (757 m3) storage tank was provided upstream of the biological plant, allowing the wastewater temperature to stabilize in the range of 150 F (65.5 C) and some suspended solids to settle. This wastewater was then biologically treated after being supplemented with phosphoric acid at a rate of 1.3 US gal of 63% H3P04 per 100 lb phenolics (11 1/100 kg). 895
Object Description
Purdue Identification Number | ETRIWC1978094 |
Title | Extended aeration of coke-plant effluents |
Author |
Ganczarczyk, Jerzy J., 1928- Elion, D. |
Date of Original | 1978 |
Conference Title | Proceedings of the 33rd Industrial Waste Conference |
Conference Front Matter (copy and paste) | http://e-archives.lib.purdue.edu/u?/engext,27312 |
Extent of Original | p. 895-902 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University LIbraries |
Rights Statement | Digital object copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Date Digitized | 2009-06-22 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Resolution | 300 ppi |
Color Depth | 8 bit |
Description
Title | page0895 |
Collection Title | Engineering Technical Reports Collection, Purdue University |
Repository | Purdue University Libraries |
Rights Statement | Digital copyright Purdue University. All rights reserved. |
Language | eng |
Type (DCMI) | text |
Format | JP2 |
Capture Device | Fujitsu fi-5650C |
Capture Details | ScandAll 21 |
Transcript | EXTENDED AERATION OF COKE-PLANT EFFLUENTS J. Ganczarczyk, Professor D. Elion, Project Engineer Department of Civil Engineering University of Toronto Toronto, Canada M5S 1A4 INTRODUCTION Activated sludge treatment of coke-plant effluents differs substantially from such treatment of sewage and many industrial wastewaters because of concentration and characteristic composition of these effluents. Biological treatment plants for coke-plant effluents are not very numerous but the technologies applied by these plants and their operation patterns also differ markedly. The activated sludge treatment plant at Dominion Foundries and Steel Limited (DOFASCO) in Hamilton, Ontario is the only Canadian plant and one of the few North American plants for treatment of coke-plant effluents. This plant is unique in its own kind because it operated without any intentional removal of excess activated sludge. During its history, the DOFASCO plant underwent few changes and in the year 1975 its aeration tank volume was doubled. The characteristic performance of this plant prior to this change and afterwards is the subject of this study. WASTEWATER ORIGIN AND GENERAL CHARACTERISTICS The coke plant at the Dominion Foundries and Steel Limited (DOFASCO) in Hamilton, Ontario produced in 1975 an average of 3,680 t/day (3,340 kkg/day) of metallurgical coke from a low-sulfur West Virginia coal. The following streams of wastewater containing phenolics and thiocyanate were collected: excess crude flushing liquor, condensate from the collection mains, condensate from primary coolers and condensate from the light oil plant. The flow of these effluents ranged from 4,700 to 10,000 US gal per hr (17.8-37.9 m3/hr) and was a function of coal moisture contents and connection of new wastewater streams to the system. These effluents were originally equalized in a storage tank of 425,000 US gal (1,609 m3) volume, which also provided a separation of residual tar. The next step of pretreatment (Figure 1) was ammonia stripping in a free-and-fixed- leg Koppers still, installed in 1971. The ammonia stripping was performed with lime addition to raise pH over 9.5, and by addition of low pressure steam at a rate of 9,000-12,000 lb/hr (4,086-5,448 kg/hr), and high-pressure steam at the rate of 700- 1,000 lb/hr (318-454 kg/hr). The additions of slaking water and steam condensates provided a 30 to 40% dilution of the wastewater. The wastewater discharged from the still had temperature in the range of 210 F (99 C), and thus required cooling during the summer through heat exchangers using bay water. A 200,000 US gal (757 m3) storage tank was provided upstream of the biological plant, allowing the wastewater temperature to stabilize in the range of 150 F (65.5 C) and some suspended solids to settle. This wastewater was then biologically treated after being supplemented with phosphoric acid at a rate of 1.3 US gal of 63% H3P04 per 100 lb phenolics (11 1/100 kg). 895 |
Resolution | 300 ppi |
Color Depth | 8 bit |
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